LB-01液体堵剂在孤岛油田中二北馆5单元现场应用

2008年 28卷 第1期
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Application of LB-01 liquid plugging agent in Zhong'erbei Ng5 unit in Gudao Oilfield
宋岱锋 贾艳平 刘玉平 韩鹏 贾斐
Song Daifeng Jia Yanping Liu Yuping Han Peng Jia Fei
中国石油化工股份有限公司胜利油田分公司孤岛采油厂, 山东东营 257231; 中国石油大学石油工程学院, 山东东营 257061
Gudao Oil Production Factory of SINOPEC Shengli Oilfield Company, Dongying 257231; Petroleum Engineering Department, Petroleum University of China, Dongying 257061
通过分析孤岛油田中二北馆5单元蒸汽吞吐热采试验区的构造特征、储层分布、储层物性、流体性质和开发现状等,选用能适应孤岛地层注汽温度的LB-01液体堵剂进行现场试验。该液体堵剂由主剂水玻璃、复合型电解质胶凝剂以及其他助剂经螯合包覆等反应形成的单液法堵水剂,具有耐高温的特征。现场共实施4口井,开井4口,平均单井日增油10.9 t、平均含水下降16.6%,累计增油4 094 t。
The structural feature,reservoir distribution,reservoir physical property,fluid property and current status of exploitation of Zhong'erbei Ng5 unit in Gudao Oilfield were analyzed in this paper.The LB-01 liquid plugging agent used in experimental area was made up of primary agent complex electrolytic agglomerating agent and other auxiliary agents.This water plugging agent was formed by chelation and encasing of soluble glass,agglomerating agent and other auxiliary agents using single-fluid method.After using this plugging agent in 4 oil wells,the average daily output were increased by 10.9 tons,average water cut decreased by 16.6 percents,and accumulated production increased 4 094 tons.
中二北馆5单元; 边水; 堵水; 液体堵剂; 现场试验;
Zhong'erbei Ng5 unit; edge water; water shut-off; liquid plugging agent; in site test;