论文详情
金湖凹陷C6断块开发调整研究
海洋石油
2006年 26卷 第2期
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Title
The adjustment research of C6 faulted block in Jinhu Sag
Authors
Ma Shujiao
Zeng Jing
Wu Jiangping
单位
中国石油化工股份有限公司江苏油田分公司试采二厂, 江苏 金湖 211623
Organization
No.2 Production Factory of Jiangsu Oilfield of SINOPEC, Jinhu 211600, China
摘要
金湖凹陷C6断块构造复杂, 储层微相类型多, 采用一套层系开发后, 油田平面和纵向矛盾突出, 油田因含水上升快而产量迅速递减, 油田过早进入中高含水阶段, 开发效果变差, 针对油田水驱采收率偏低的现状, 采用地质、物探、油藏工程等专业联合攻关, 研究潜力方向, 提出了细分层系调整的思路, 进行了注采井网的调整, 取得了较好的效果。
Abstract
The structure of C6 faulted block is complicated, the type of sedimentary microfacies is various, and horizontal and vertical heterogeneity were serious during adopting a stratum development. The output of oilfield fell quickly because water cut had risen, oilfield had prematurely entered the middle-high water cut stage, and development effect became poor. Aiming at low water displacement recovery, we use geology, reservoir and exploration to research oil potential. The technique of the subdivision of series of strata development is also used to adjust well pattern, and this adjustment achieves superior result.
关键词:
沉积微相;
层间矛盾;
细分层开发;
井网调整;
Keywords:
sedimentary microfacies;
vertical heterogeneity;
the subdivision of series of strata development;
well pattern adjustment;