埕北322井井斜过大的原因和随后采用的技术

2003年 23卷 第2期
阅读:119
查看详情
Causes of Abnormal Inclination Build-up and Following Techniques in ChengBei 322 Well
何剑宏
HE Jian-hong
中国石油化工股份有限公司 上海海洋油气分公司, 上海 200120
Shanghai Offshore Petroleum Branch, SINOPEC, Shanghai 200120, China
文章介绍了埕北322井钻遇的地层特征,采用的井身结构,以及钻进中引起的复杂情况,阐述了造成井斜过大的原因和PDC钻头使用中存在的不足,提出了避免井斜过大须采取的技术措施和在该地区钻井钻头合理选型的建议。
This paper briefly introduces the formation characteristic and the casing structure in ChengBei 322 Well, as well as downhole problems occurred during drilling through 311.2 mm section. And it also describes the causes of abnormal inclination build-up and deficiencies of using PDC bit. Some suggestions are brought forword on how to prevent from abnormal inclination build-up and how to select PDC bit in that area.
埕北322井; 明化镇组; PDC钻头; 井斜;
ChengBei 322 Well; MingHuaZhen formation; PDC bit; inclination;