渤南油田注采二次不完善状况分析及对策研究

2006年 13卷 第06期
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Analysis of Secondary Incompletion of Inject ion-Production Pattern and Relevant Countermeasures in Bonan Oilfield
高保国1 盛立江1 蔡勇胜1
( 1 胜利油田分公司河口采油厂, 山东东营257200; 2 胜利油田分公司地质科学研究院, 山东东营257015 )
 Hekou Oil Production Plant, Shengli
O ilfield Company, SINOPEC, Dongying 257200,
China
渤南油田低渗透油藏注采井网二次不完善, 削弱了油田稳产基础。通过注水井
数及注采对应率变化规律研究, 分析了造成水井停注的因素, 指出水质不合格和套管损坏是注
采井网二次不完善的主要原因, 提出了水质精细处理、油层改造和油井转注等针对性的治理对
策。实施后注入水水质明显改善, 增加和恢复有效注水井点43个, 开发效果显著好转。
Founda tion o f stab le production o f low perm eab ility
reservo ir, in Bonan O ilfie ld, is underm ined by incomp le tion
o f injection - produc tion pa ttern. It has been found, by
study ing the va riation laws of num ber o f injection we lls and
change of co rresponding ra te of injection-production,
analyzing the factors affec ting in jection w e lls, tha t the two
ch ie f reasonss causing the incomp letion are g iven. Such
proposa ls, such as the fine treatm ent of wa ter, m odifica tion o f
o il bed and transform ation of production w e l,l we re proposed.
A fter these m easu rem ents have been taken, the w ate r qua lity
has been obv iously im proved, 43 effic ient in jection locations
have been improved or restored and the production effects
have becom e outstanding ly w el.l
渤南油田; 低渗透; 注采完善; 污水处理;
Bonan O ilfield, Low perm eability,
Com pletion o f injection-Production pattern, W aste wa ter
treatment.;