扭力冲击器在宋深9H 侧钻小井眼水平井中的应用

2014年 36卷 第6期
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Application of TorkBuster to sidetracking of slimhole horizontal well in Well Songshen 9H
陈鑫 陈绍云 王楚 李瑞营
CHEN Xin CHEN Shaoyun WANG Chu LI Ruiying
东北石油大学,黑龙江大庆 163318 大庆钻探工程公司钻井工程技术研究院,黑龙江大庆 163413 大庆油田有限责任公司采油一厂,黑龙江大庆 163001
Northeast Petroleum University, Daqing 163318, China Daqing Drilling Engineering and Technology Research Institute, Daqing 163413, China No. 1 Oil Production Plant of Daqing Oilfield Co.Ltd., Daqing 163001, China
为提高庆深气田侧钻小井眼水平井钻井速度,缩短钻井周期,开展了扭力冲击器配常规导向动力钻具提速技术的研究与应用。首先,重点分析新钻具组合强度是否满足钻进需求,从而防止应力集中造成钻具疲劳破坏;其次,利用扭力冲击器泵压- 排量回推公式,优化钻井参数;最后,按照钻具允许的弯曲半径必须小于井眼/ 套管实际弯曲半径的原则,分析了?215.9 mm 和?152.4 mm 钻具组合通过能力,从而实现了钻具安全下入,形成了庆深气田扭力冲击器小井眼水平井提速技术, 并在宋深9H 井成功实施,为加快深层砂砾岩气藏的勘探开发提供了新的技术手段。
In order to improve drilling rate in sidetracking of slimholehorizontal well in Qingshen Gasfield and shorten drilling period, research and application has been conducted on the technology of increasing drilling rate by TorkBuster assisted with conventional geosteering power drill. Firstly, analysis was conducted to see if the new assembly had enough strength for drilling, thus preventing fatigue and damage of the drillstring caused by stress concentration; secondly, the TorkBuster pump pressure-displacement back-push equation was used to optimize the drilling parameters; finally, the passing capacity of ?215.9 mm and ?152.4 mm assembly was analyzed as per the principle that the allowable bending radius must be less than the actual bending radius of slim hole/casing, hence realizing safe running of the assembly and generating this technology for increasing drilling rate in slim hole horizontal well by TorkBuster in Qingshen Gasfield, which was successfully used in Well Songshen 9H, providing a new technical approach for accelerating the exploration and development of deep sandy conglomerate gas pools.
庆深气田; 扭力冲击器; 水平井; 小井眼钻井; 宋深9H 井;
Qingshen Gasfield; TorkBuster; horizontal well; slim hole drilling; Well Songshen 9H;
10.13639/j.odpt.2014.06.008