务古4井复杂深井钻井液技术

2012年 34卷 第6期
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Complex deep well drilling fluid technology for Well Wugu-4
赵江印 陈永奇 刘志广 贾思航 周锋 周春阳
ZHAO Jiangyin CHEN Yongqi LIU Zhiguang JIA Sihang ZHOU Feng ZHOU Chunyang
渤海钻探工程公司第四钻井工程分公司,河北任丘 062552 华北油田公司第三采油厂,河北河间 062450 华北油田公司第一采油厂,河北任丘 062552
No.4 Drilling Company, BHDC, Renqiu 062552, China No.3 Production Plant, Huabei Oilfield Company, Hejian 062450, China No.1 Production Plant, Huabei Oilfield Company, Renqiu 062552, China
务古4井为一口重点探井,完钻井深5 750 m。该井二开裸眼井段钻遇巨厚层泥岩,选用聚磺钻井液体系,解决了地层严重造浆及井眼稳定问题;三开裸眼井段存在多套压力系统和多处断层,钻遇石膏、含膏泥岩、大套玄武岩以及凝灰岩和碳质泥岩等地层,特别容易发生坍塌和井漏,井壁极为不稳定。现场采用有机盐钻井液体系,有效解决了石膏、膏泥岩污染和严重井壁垮塌导致的大段划眼、严重蹩钻及遇阻卡等复杂问题;添加低渗透处理剂和屏蔽暂堵剂及复合堵漏剂,提高井壁的承压能力,解决了三开施工出现的压差卡钻风险,确保了钻井安全顺利,完井电测一次成功,钻井周期大幅度降低。
Well Wugu-4 is a key exploration well with total depth of 5750m. During drilling the 2nd interval open hole, thick mudstone was penetrated. Polysulfonate drilling fluid was taken to solve the serious mud-making and wellbore stability issues. For the 3rd interval, multiple pressure system and faults were encountered, and plaster, plaster mudstone, huge basalt, tuff, and blacks were penetrated, which makes it prone to collapse, leaking and wellbore instability. Organic salt drilling fluid was taken to slove the issues of reaming down, bit bouncing, bit sticking, etc. The low permeability additive, temporary blocking agent, and sealing agents were added to improve wellbore pressure bearing ability. The risk of bit sticking from pressure difference during the 3rd interval drilling was solved and drilling safety was ensured. The completion logging was successful with only one run, and the drilling cycle was decreased significantly.   
深井; 聚磺钻井液; 有机盐钻井液; 井壁稳定; 务古4井;
deep well; polysulfonate drilling fluid; organic salt drilling fluid; wellbore stability; Well Wugu-4;