官69-19井微生物吞吐试验研究

2002年 24卷 第2期
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STUDY ON MICROBIAL BUFF AND PUFF TESTING OF GUAN69-19 WELL
陈聚顺 闫宝东 张晓弟
Chen Jushun Yan Baodong Zhang Xiaodi
大港油田公司油气勘探开发技术研究中心, 天津大港 300280
Research Institute of Exploration and Development, Dagang Oilfield Group Co. Ltd
通过对传统采油微生物筛选方法的改进,结合官69- 19井的地层特点筛选出嗜高温(65~100℃)菌种和针对高矿化度油藏的营养体系。为验证菌种和营养体系的矿场试验效果,并为今后嗜高温菌种大规模应用于高温、高矿化度油藏积累经验,对官69-19井实施了井筒和近井地带的微生物处理试验。结果表明:井筒处理后,原油产量由3.17t/d上升到5.3t/d;近井地带处理后,产量由3.17t/d上升到5.04t/d。说明试验是成功的,有利于今后在高温、高矿化度油藏的进一步推广应用。
According to the stratum character of Guan69-19 well, a best-liking high temperature(65~100℃) bacterium and a new nutriment system aim at high salt oil reservoir have been filtrated out through improving on the traditional methods of filtrating petroleum microorganism. Using the bacterium, wellbore and near wellbore area microbial testing has been done to validate the effect. The accumulate experience for the cosmically application on high temperature and high salt oil reservoir. The result indicates that the production has been rise from 3.17 tons per day to 5.3 or 5.04 tons per day. All that shows the testing is successful and it will be benefit to expand application in high temperature and high salt oil reservoir.
嗜高温菌种; 微生物吞吐; 井筒; 近井地带;
Dagang Oilfield; microbe oil recovery; huff and puff testing; wellbore;
10.3969/j.issn.1000-7393.2002.02.022