北12X3井?139.7mm套管固井技术

2001年 23卷 第2期
阅读:74
查看详情
CEMENTING OF?139.7mm CASING IN WELL BAI 12X3
白亮清 冯京海 李祥银 赵树国
中国石油冀东油田监理公司, 河北唐海 063200
Supervising Co. of Jidong Oilfield, CNPC
北 12X3井是 1口重点探井,实际完钻井深 44 15m。该井三开钻井过程中,井下出现了坍塌、掉块、井漏、气侵严重等复杂情况,造成三开井段井径极不规则,给固井施工带来很大的困难。通过强化固井准备、优化固井设计、优化水泥浆性能,严格细化技术措施,较好地解决了施工中存在的问题,固井质量达到设计要求。
Well 12X3 is an important exploration well drilled in Jidong Oilfield, with an actual total depth of 4415m. During the drilling of ?215.6mm hole, well collapse, cutter lost, lost circulation and gas invasion frequently occur, and an irregular hole profile is build, which is very bad for cementing operation. In this case, a lot of preparation work is carried out, and the cementing program, as well as cement slurry properties, are modified to meet the actual downhole condition. During the field operation, the procedures are strictly followed, and a successful cementing job is completed.
冀东油田; 固井; 井漏; 设计; 施工;
Jidong Oilfield; cementing; lost circulation; design; operation;
10.3969/j.issn.1000-7393.2001.02.007