杏南油田注聚井堵塞原因及解堵剂配方研究

2016年 29卷 第No.2期
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Blockage Reason of Polymer Injection Wells in Xingnan Oilfield and Determination of the Plug Removal Agent Formula
(东北石油大学石油工程学院,黑龙江大庆163318)
 

(College of Petroleum Engineering, Northeast Petroleum University, Daqing Heilongjiang 163318, China )

关键词: 聚合物, 注聚井, 注入压力, 堵塞, 解堵剂
According to the problems of that the serious blockage of polymer injection wells, the high injection pressure and the bad effect of polymer injection in Xingnan oilfield, the polymer and water of a block in Xingnan oilfield was adopted to carry out the laboratory experiments on simulation of polymer flooding and plugging and then the reason of blockage was found out. The results show that the polymer and mechanical impurities are the main factors to cause the pore blockage, and the lower the permeability, the more serious the blockage. Aiming at the blockage reason, laboratory experiment study on the formula of plug removal agent was carried out. Finally the multiple plug removal agent consists of agent A, B and C was determined. On the basis of optimizing the mass fraction of each agent, the injection volume and the injection order, the broken down rate of formations can reach 102.41%~124.77% with this plugging removal agent formula.
聚合物; 注聚井; 注入压力; 堵塞; 解堵剂;
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黑龙江省自然科学基金重点项目“活性原油在非均质储层中的自适应控水增油机理”(51574089)。
10.3969/j.issn.1006-396X.2016.02.007